A SUCCESSFUL EXPERIENCE IN OPTIMIZATION (一个成功的优化经验).pdf

A SUCCESSFUL EXPERIENCE IN OPTIMIZATION (一个成功的优化经验).pdf

  1. 1、本文档共13页,可阅读全部内容。
  2. 2、有哪些信誉好的足球投注网站(book118)网站文档一经付费(服务费),不意味着购买了该文档的版权,仅供个人/单位学习、研究之用,不得用于商业用途,未经授权,严禁复制、发行、汇编、翻译或者网络传播等,侵权必究。
  3. 3、本站所有内容均由合作方或网友上传,本站不对文档的完整性、权威性及其观点立场正确性做任何保证或承诺!文档内容仅供研究参考,付费前请自行鉴别。如您付费,意味着您自己接受本站规则且自行承担风险,本站不退款、不进行额外附加服务;查看《如何避免下载的几个坑》。如果您已付费下载过本站文档,您可以点击 这里二次下载
  4. 4、如文档侵犯商业秘密、侵犯著作权、侵犯人身权等,请点击“版权申诉”(推荐),也可以打举报电话:400-050-0827(电话支持时间:9:00-18:30)。
查看更多
A SUCCESSFUL EXPERIENCE IN OPTIMIZATION (一个成功的优化经验)

Archive of SID Iranian Journal of Chemical Engineering Vol. 6, No. 2 (Spring), 2009, IAChE A Successful Experience in Optimization of a Production Well in a Southern Iranian Oil Field S. R. Shadizadeh, M. Zoveidavianpoor∗ Petroleum University of Technology Petroleum Engineering Department, Abadan, Iran Abstract Production optimization ensures that wells and facilities are operating at their peak performance at all times to maximize production. This paper describes a procedure, to develop Inflow Performance Curves, Tubing Performance Curves and Choke Performance Curves, for one of the Iranian southern oil wells, from the results of a multiphase flow simulator (PIPESIM). The goal of this project is to optimize the production from one of the southern Iranian oi l fields. Increasing the choke size leads to maximizing production, and causes an optimum reduction in wellhead pressure and bottomhole flowing pressure. Controlling flow patterns in all sensitivity analysis play a major role in selecting the proper variables. Using 7in. OD tubing size rather than 9 5/8 in. casing size and selecting 9/16 in. choke size rather than 7/16 in., the wellhead pressure between 700 to 1180 psia will be the result and

您可能关注的文档

文档评论(0)

jiupshaieuk12 + 关注
实名认证
内容提供者

该用户很懒,什么也没介绍

版权声明书
用户编号:6212135231000003

1亿VIP精品文档

相关文档